Over the last week I made a few parts on my CNC, one of which was made out of aluminum. The first part was a replacement part for a VR headset a friend gave to me. I accidentally broke one of the 3D printed adjustment racks and had to make a new one.
I made it out of HDPE, which is just wonderful to machine, due to its flexibility. I surfaced the material to thickness and cut out most of the profile with a 1/8" endmill. I used a cheap 1/16" endmill to get between the rack teeth:
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Surfaced and most of the internal surfaces cut out. |
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Completely cut out. |
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Replacement on the left. |
The next part I made was out of aluminum. This was a bearing block designed to replace the original wooden ones I made not too long ago. I didn't use any oil/coolant and it went fairly smoothly. Next time I probably would get rid of the lead in and lead out on the 2D contours and just use ramps. The plunge between each depth didn't sound great.
I used a 2 flute, 1/4" endmill for the whole process:
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Sharp. |
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Cut out. |
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Reasonable surface finish. |
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After cutting, the part was square as far as I could tell and had reasonable dimensional accuracy. The CAD model was 2.953" by 4.035", and part came out to be 2.960" by 4.034".
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Square. |
The hole cut out for the bearing was supposed to be 1.126" in diameter, but when I measured it it ranged from about 1.123 to 1.125. Had I taken a finishing pass I probably could have gotten closer and the bearing would have fit in. I had to sand the inside of the cutout with a Dremel to be able to get the bearing to fit.
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Installed.
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